SuperSpec

SuperSpec

Sunday, 19 March 2023

Traumatic Journey

 Today was one of the regular coffee/cake mornings at Great British Sportscars (GBS).   The weather looked a bit dodgy, but the radar picture showed I should be OK, so I decided to go.

First problem was that she wouldn't start.  She cranked at full speed  but didn't start.   I tried 3 times but with no success.  I was going to give up, but on the 4th attempt she coughed a bit so I tried one last time.   This time, after about 5 seconds of cranking she started, coughed twice and settled down to a nice idle.  (Postscript:  I haven't managed to reproduce this at all, she continues to start with no problem)

So for the first 50 minutes all was fine, but then, with about 8 miles to run I ran into a terrible rain storm.  Luckily I was doing 65mph on the A1 so was totally protected, but visibility was awful and the rain terrential.   Came out of that just as I turned off  the motorway.  As I went through a village the temperature started to climb so I switched on the fan.  Nothing, dead as a door nail.   At the same time I noticed the alternator voltage was down to 13.2V from it's normal 13.8V.   I only had about 5 miles to run so I decided to keep going, assuming that I might have to call AutoAid to get back home.

Soon after I arrived (with the engine temperature in the red) it started raining again so I quickly put the top up.  After an hour or so I decided I would have to make a move.   First step was to fill up the coolant so I put the umbrella up and took the bonnet off.   To my surprise the coolant level was OK, so didn't need topping up.   Next (nice) surprise was when she started instantly.

So drove home down the A1 so rain didn't affect me, trying to keep the engine temperature down.   Apart from a couple of scares when I saw queues building up I managed to make it.

The fan was fixed in under a minute as it was a broken earth.

So panic over but not a journey I enjoyed.


Tuesday, 7 March 2023

Back on the road

 It took a couple of weeks but she is back on the road.   I was able to buy a new pump/sender off EBay for £32 as it is a standard Ford part used in the Escort/Fiesta/Ka.   My initial attempts to remove the old one were unsuccessful as it was corroded in place.  But once I bought the proper removal tool it came off easily.   Not unexpectedly, the union for the fuel pipes was a 'bodge'.  Rather than using the official right angle join they had simply pushed the fuel pipes in.

*GENUINE* FORD KA FIESTA FUEL PETROL PUMP PIPE HOSE CONNECTORS (ONE PAIR)  

It was very difficult to get them out and in the end I cut then off to get the unit out.

Once in, and taking advantage of the access to redo the fuel couplings, she was up and running.

 

Tuesday, 24 January 2023

It had to happen eventually

 It was inevitable that at some point the car would break down and I would need to call out the breakdown service.   At least this one was very simple.   I was leaving for a meet up with some other owners when, after only 2 miles, the engine cut out and I rolled to a stop.   Luckily I was on a country road with very wide grass verges so I pulled off onto the grass, well clear of any traffic.

I very quickly found the characteristic 2-sec burst from the fuel pump when you switch on the ignition wasn't happening.   The fuel pump relay had previously stuck so the first thing I did was swap over the relay with the horn relay.  That didn't help so I checked all the fuses and the wiring to make sure thet were OK.

At that point I realised it wasn't going to be a quick fix so I called up AutoAid who I had a policy with.  Very impressive service, a rescue van pulled up after 45 mins.  The driver had worked on kit cars so he wasn't fazed by the 'rats nest' I call a wiring loom.  He ran all the checks I had done and also diagnosed the fuel pump.


So it was time to get the towbar out and drive me back home.

(We had to remove the nose cone to find somewhere to put the towing arm)

I was lucky to be in a suitable location on a reasonably nice day (no rnain if a bit chilly) on a journey that wasn't essential.

Now to fix it.

Tuesday, 29 November 2022

Trivial Problems

 Not surprisingly I have cut back on the drives, although I won't be SORNing the car as there are still the occasional days when it's lovely to be out.    The other problem is that it is very cold in the garage and not conducive to working on the car.  As such I am carrying a couple of nagging problems I really ought to check out.

A couple of trips ago I felt I was having to press the throttle further down than usual so decided to have a look.   The reason was obvious when I took the bonnet off:


The adjuster nuts had vibrated loose and travelled apart and I was actually lucky the cable was still inside the gate.    It seemed a quick fix, but when I tightened it up I found she was idling at around 2000rpm instead of 1000rpm.   I tried adjusting it, but it is very difficult to do as the engine needs to be fully warmed up before the genuine idle speed is obtained.   At the moment I have it down to 1400 rpm so it still needs work,

I am still losing water, although very slowly.  It just means I have to top her up every 200 miles or so.   I've accessed all the pipes I can get at and none of them are showing any synptoms of a leak.   However I haven't checked the connections under the expansion bottle as that needs accessing from underneath.   However, in the last few trips I have felt water (or fuel ?)  dripping onto my left ankle as I drive away from the house.  Unfortunately the expansion bottle is on the passenger side of the car and at first glance I cannot see how any water could move across the car to the driver side.   I'll have to put her on extended axle stands so I can do a proper check.   But is is sooo cold 😀

Wednesday, 12 October 2022

Minor fixes

 Time to fix the 2 problems identified at Corby Glen.   First I looked at the clutch switching on the brake light.  My first attempt was to spray the pivot points of both the clutch and the brake pedals, and loosen off the bolt they are mounted on.   That didn't help so I loosened off the brake light switch and moved it a couple of mms away from the brake pedal.   That worked, although the light doesn't come on unless I am positively braking, but that is fine.

Second was the reversing lights and sensor not working.  The common factor here is the reversing switch fitted to the gearbox so I put her on axle stands and went underneath.  I didn't have to search very far for the reason:


The yellow wire was firmly attached, the red wire was floating free.

So I just plugged the red wire in and checked again.   The lights started working but after a few seconds failed again.

I tried shorting the wires and the lights and sensor starting working, so it meant that either the switch had failed or the connections weren't making.   A quick check with a multi-meter showed the switch was fine.   So I rewired the spade connectors with brand new ones, plugged them in and everything was fine.

Good job done.

Monday, 10 October 2022

Corby Glen Sheep Fair

 As usual at this time of year we were invited to show our cars at the Corby Glen Sheep Fair.   As it is only 1.5 miles from me I can't refuse 😅

The weather was perfect so we had a huge turn out of visitors and cars.  In fact I actually moved from our normal place further along the road so we had plenty of room.  We had 5 cars and were joined by a Caterham Seven:


 It was a lovely day except one of the drivers who had been following me said my old problem of the clutch operating the brake lights has returned.   I also noticed ny reversing sensors weren't powering up and the drivers confirmed my reversing lights weren't coming on.   Hopefully easy fixes.

Thursday, 18 August 2022

MOT Time

 It's that time of year again 😅  I never look forward to it as while I can make sure 90% of the car is ready I can never predict what the emissions test will throw up.   I was also a bit worried about the sump guard.   A few years ago they ripped my Mk1 version off when using the rollers for the brake test.   Last year I removed the Mk2 version just before the MOT and they managed to hole my sump.

So this year I gave her to my mechanic, who checks her over before taking her to the local garage and asked him to remind them to be careful with the rollers, and also to make sure she was well up to temperature before they did the emissions test.   He mentioned that a couple of his vehicles (4x4) could not be tested on the rollers and that they did a 'tap' test, which involves putting a decelerometer in the car and then driving it round the block and tapping on the brakes.   Sounded good to me.

So off I went to wait at home, but a couple of hours later I got a phone call to say that the tester had got a bit carried away with the emissions test and had run her so hot a cooling hose had blown off and filled his inspection pit with hot water/antifreeze.   My mechannic said he would take his trailer down, bring her back and try and fix her.   Next phone call was a couple of hours later to tell me she had passed with flying colours with no advisories and was ready for pick up.

At the same time I had asked him to fit my new speedo cable, as fitting the gearbox end requires the car to be up on a lift to get access to it.   He fitted it, but unfortunately I found on the way home that the speedo still didn't work so we aren't there yet.

More on that later.

Tuesday, 10 May 2022

Kit Car Shows

 I haven't put in a post for some time as she is running perfectly and hasn't required any fettling.    The lambda sensor suddenly started working again.

But I have still been busy, I took her to the regular 'Cakes & Coffee' meeting laid on by Great British Sportcars (GBS).   I also took her on the Stilton Cheese Run, for the 7th year and finally down to Stoneleigh for the Annual UK Kitcar Show.   The mileage is piling up and I have now passed 26,500 miles.

Good times.

Tuesday, 22 March 2022

Lambda Sensor (Again)

 

During the GBS trip I decided to do an instrumented run to check the lambda sensor.   I noticed straight away she didn't go into closed loop so after a few miles, while at some traffic lights, I stopped the engine, counted to 10 and restarted her (good thing we don't suffer from the hot starts any more).   She quickly went into closed loop and stayed there for the rest of the trip there.  


Here's the trace. 
As we can see she was scruffy as old boots until the restart and then absolutely fine.  

On the way back the same thing happened, except this time the first attempt at restarting didn't help.  It was a second, later, attempt, again at some traffic lights, that made the difference.,

So what can we deduce from that ?   Although the sensor could be going soft, my first thought is that the heater is not working properly.  As we know my wiring is not the best in the world 😁 I guess while I have the soldering iron out I can redo all the lambda heater joints.   I'll see how that goes.    But there's no mad rush as I don't need it working till the emissions test in August.

Monday, 21 March 2022

Cooling OK ?

 

During the trip to GBS I had a chance to check the cooling

 

And there was good news.    Here we have her on the way there.  She sat at 85C for the first 2/3rds of the trip.  The blip was when I hit a traffic hold up at the junction of the A17 and A1.  It wasn't enough to trigger the fan and as you can see it rapidly came back to normal when I hit the open road.

And here she is on the way back.  Again a solid 85C.   Although this is a bit deceptive.   At the point where the intake temperature blips I had pulled into Grantham to get some fuel.  As an experiment I switched on the fan as I was in the 30mph zone and that was the result.  

When I got back there was no water in the overflow bottle and the water level was unchanged (and I was bit concerned to find I had forgotten to bolt the nosecone in, it was simply held in position by the bonnet resting on it).  So that is a relief, it means I don't have a leak or a blown head gasket (doesn't mean I shouldn't check it before every trip though😁).   I'm still not convinced that the seal between the pressure cap and the expansion bottle isn't a bit dodgy.  I added an extra rubber seal yesterday to see if that helped.  It may have done.   I also might start getting into the habit of switching the fan on if I can see an obvious trouble spot coming up, or traffic lights or a 30mph speed limit.   It is obvious now that once she gets too hot she starts dumping water and that makes her get even hotter.   Better to prevent her getting hot in the first place.    Or maybe revert back to a 92C fan thermostatic switch from the present 95C one ?

A couple of minor glitches, the carpet on the passenger side won't stay up any more, needs redesigning (not what you would call critical 😁), I think the clutch cable needs adjusting a bit, had a couple of occasions when I couldn't get into second, and someone pointed out that my offside DRLs weren't lighting up.   I have been thinking I would rewire them properly anyway so the soldering iron comes out tomorrow.


Saturday, 19 March 2022

GBS Coffee & Cake

 Every few months Great British Sports Cars (GBS)  host a kit car meet at their factory.  GBS took over the Robin Hood fircoolm when it folded and still support the cars so I often attend the meets.   The weather today was fantastic, and I needed to check the cooling system so I decided to go. 

What a cracking drive, 75 miles in total.  Weather fantastic although cross wind on the A1 a bit rough (Only did 7 miles on the A1 though).   Also the sun is now high enough so I don't get blinded on the way back South (which is a good thing as my sunscreen blew off yesterday and was destroyed by the car behind 😁).

Never seen it so busy, there were a huge number of cars, the forecourt was full and cars were parked both sides of the approach roads for 100 yards.    Predominately Zeros, but lots of other kit cars of all shapes and sizes.  Free coffee and the best selection of cakes and biscuits I have seen for some time. 


I must admit that much as I love the Superspec I have a sneaking regard for the Ariel Atom:

Perhaps I could imitate it by taking all the side panels off 😁

 

 

 

I had to park on the road.   Turned out to be a good thing as I could leave when I wanted as most people on the forecourt where stuck there for the duration.   She was probably the oldest car there, all the others looked brand new in showroom condition, she still attracted a few people though so I was kept busy chatting.ng. 

Friday, 18 March 2022

Rebushing

After the MOT failed with 2 of the front suspension bushes we decided to replace all the rest.   While she was in I asked the mechanic to fit some new shock absorbers I had been given, fit a new speedo cable I had found on EBay, and fit a new rear exhaust mounting that had sheared on the way to deliver the car.

 So picked her up today and we had about a 60% success rate 😁 Front end now completely re-bushed but he said there was no point in doing the tracking until I had driven a few miles to let the suspension settle.   But he did say that one of the wishbones was a bit loose with the old bushes so that may have contributed.   On the drive back she still pulls to the left a bit but nowhere near as bad as before.   He recommended a garage he uses to get all his car tracking checked, so I might do that in a few weeks.   He hadn't fitted the shock absorbers, initially he was worried that springs were a different colour (green rather than blue) which means the strength was different but then on close examination the bottom mounting was slightly wider than the existing ones so wouldn't fit.  

He also hadn't managed to fit the new speedo cable.   Again, at first it looked identical and I had checked that the instrument end as that looked different.  Turned out it was the correct version and fitted perfectly and the original one was the wrong fitting so it could only be pushed in half way.    That explained why it kept coming out.  What we didn't realise was the gearbox end, while looking identical and supposedly for an MT75, was very slightly thicker so when It was pushed in there wasn't enough clearance to fit the circlip.   So he just fitted a blanking plate to the hole, something I have been thinking of doing.   I'm in 2 minds now, I have lived without the speedo for almost 3 years now without any problem.   Or I could go to a firm that build cables and get a bespoke one made up with the gearbox end of the old one and the instrument end of the new one.    But that would be quite expensive.    We'll see.

Finally he had put a temporary solution on the exhaust mount. Unfortunately he has done such a good job I think it might be another case of a short-term fix becoming a long-term solution 😁



Wednesday, 16 March 2022

Coolant Problems (again)

Weather was good so it was a good time to have a picnic, so we went to Burghley House on Tuesday.   

Nice day but on the way back I happened to notice the temperature gauge firmly in the red.    Pulled of the road and shut her down.   It sounded like a kettle boiling in the engine.  Sure enough, when I took the bonnet off the system was boiling like mad and coolant was pouring out of the overflow.   After the original problems I have always carried a 2 ltr bottle of water in the passenger footwell.   My only concern was how long I had to wait before I could take off the pressure cap.   I was a bit surprised when I felt the cap and it wasn't hot.   So I risked taking it off, and after a few seconds of releasing the pressure it came off.    So put the 2 ltrs in and started again.   It seemed to be OK but 6 miles from home it shot up into the red again.   Luckily I had stopped in a small village and a friendly house owner filled my bottle up for me and that was enough to get me home.   So I have kept up my record of never arriving home on the back of a rescue truck 😁

So filled her up, using the top of the radiator outlet to make sure I got rid of all the air.   Drove her today, 11 miles each way and the needle didn't even get to the 'N'.    Once she has cooled off I will check the water level and make sure I don't have a new leak.   I hadn't checked the water level for months, so I think it just gradually gone down until it was suddenly below the water pump and the sensor and then it just shot up to the red as the circulation stopped.   That would explain why the pressure cap was cold and also the engine definitely did not feel it was excessively hot.



Friday, 22 October 2021

New Battery

 Although I tend to put the battery on a trickle charger a day before a trip, I found that starting was becoming very sluggish.   And the voltmeter was showing that during cranking the voltage was dropping dramatically.   It's over 4 years since I had a new battery do decided it was time to get a new one.

First problem I had is that the connections I use are designed to fit a square terminal rather than the more usual post terminal.   Also the battery tray is a bit smaller than the usual, so a standard 243mm length battery will not fit.  I cannot go above 210mm.

The result was that I could not find a suitable replacement.  On the other hand Europarts had a battery of the required size, but with post terminals.  Also they had a 'winter discount' that reduced the cost from £99 down to £53.   


A quick search on Amazon showed these, perfect adapters.

Once I relaised they were different sizes they fitted perfectly.

Job done.

Thursday, 23 September 2021

Lambda Sensor again

 While I was celebrating the MOT pass I was hit with lambda problems again.   As regular readers will know, a failure of the sensor is almost unnoticeable as the car performs normally.   But purely by coincidence I decided to do an instrumented run.   The log immediately showed the problem, in that the lambda sensor voltage was firmly fixed at 435mV and the whole journey was in open loop.

Although I had rewired the system a few months ago I really didn't like my solution so thought it was time to rip it all out and start again.  So the first step was to rewire the heater from where it left the loom.  Before plugging in the sensor I checked that the voltage output was zero until you started the engine then it jumped to 13.5V as the alternator kicked in.

Next I replaced the signal wires with 2 separate screened cables, one for the signal and one for the earth.  Probably overkill, but I happened to have  some single-core screened cable I could use,

So all plugged in I started the engine and plugged in MEMSScan to monitor the lambda voltage.  Unfortunately it stayed at 435mV, although after 3 mins or so it gradually crept up to 450mV, so something was obviously still wrong.

Not sure why I did it but I retested the  heater wires unplugged and found they were still showing 13.5V,  but when I plugged in the sensor the voltage dropped to 0.11V.   So offload it was OK, but under load it was failing.   Next step was to swap the sensor for my spare, but that didn't help and the same happened.

I needed to get her on the road so as a short-term measure (although I am the first to admit my short-term fixes have a tendency to become long-term)  I provided a new feed to the heater using a dedicated earth and an ignition switched 12V.   The downside to that is that the heater is activated immediately you turn on the ignition rather than waiting till the engine is running.   I just have to make sure she doesn't sit with the ignition on for very long.

MEMSScan appeared to show that now everything was working.   So took out for a long run and here was the log file:


 Happy days 😁

So I still don't know why the voltage dropped dramatically when the sensor load was added, I need to investigate that further.

I also now know that the sensor will NOT work unless the heater is on, even when the engine has warmed up to temperature.